Head- and foglight (82)
Head light
Partly restored Bosch headlights
The head lights were, as many other parts on my car since my father cared for it, in good shape. I still decided to re-chrome all chrome parts and repaint and/or re-plate the other parts. Retaining springs, sealing rings for the glass as well as parts necessary for the light adjustments were bought new. The reflector I diagnose as being enough bright as they are, not needing restoration.
The supporting ring, the black and silver painted ring that the headlight is sitting in, was a candidate for repaint. I didn’t want to destroy the original markings on top of it, and don’t have the means to re-create them yet, so I covered them up instead. After that it was just a matter of sandblasting the ring and then paint it in silver and semi-gloss black. The adjustment ring, as I call it, had to be sandblasted, plated and repainted. The adjustment screws, with their locking mechanism, were removed and replaced. The purpose of the locking mechanism is to hold a small spring tight enough towards the black adjustment ring (i.e. the black, flat ring) so that the adjustment screws are not moving while driving, i.e. changing the horizontal or vertical adjustment of the headlight.
Below you can see the sandblasted, and then plated, adjustment rings as well as a box with ornamental rings and light pots, cleaned by the chrome shop and awaiting polish. I did what I could here but I let the chrome shop do the final polishing.
In the next gallery you can first see some of the new items for the light adjustment as well as the painted supporting ring. I also deliver some pictures of rechromed ornamental ring for the Bosch headlights as well as the fastening screws.
All parts ready for assembly can be seen in the first picture. Almost all… For the Bosch head lights you use 8 retaining springs per side (Hella uses four per side and they are probably different in their shape) something I realized after this picture was taken. More about that later. In the second picture below you can see the new ”nuts”, and their rubber support, for the horizontal and vertical adjustment screws. The third and fourth picture show the adjustments screws. As you can see in one of the galleries above the original locking mechanism had to be removed. Unfortunately, the new locking mechanism consists of two counter-tightened nuts per screw. I say “unfortunately” since the two nuts together, get too thick and are in the way during the later assembly of the lights in the fender. The adjustment and ornamental rings where rust protected on the backside. The sealing ring around the glass goes with the grooves forward, towards the adjustment ring.
It took a while to understand how the retaining springs were to be assembled. The springs are very hard and supposed to go in between the edge of the adjustment ring and a groove in the supporting ring. The spare parts list said 8 per side but it was impossible, the springs flew all over the place or the two rings separated. I asked around on my forums and most said they had had no problems. After some "digging" it turned out that there were mostly two reasons behind that; either they used fewer springs than 8 or they used old springs. With the new springs I had to have something that hold the whole package together while inserting them. That fixture is what you see in the second picture. If you use too few, or old, springs you run the risk that the glass, supporting ring and reflector with lamp is not held together hard enough. If someone leans towards the lamp it risks being pressed into fender. One of the respondents had actually experience of just that. Also stories of headlights that had fell into the fender while driving was told. Now I and they know the reason behind that.
With the fixture it got easier, only almost impossible to insert the springs. The springs need to cross each other in order to sit tight, you also need to adjust their place so that they don’t block the lower screw hole or come in contact with the adjustment screws. It takes some time to move them back- and forward until everything is in place.
Foglight
Restored Bosch foglights
I went for the same procedure with the fog lights as with the head lights. The car was actually equipped with Marshall fog lights from the beginning. Or rather, my father bought them on the aftermarket after the car was delivered to him. They look something like the ones in the gallery below. To me they didn’t look that good on the car, too large diameter. Hence, I decided to go for the “standard”, smaller Hella/Bosch fog light. I got this pair as part of a repayment of a debt.
They were in a decent shape as well but as usual I took them apart and had everything cleaned, re-chromed, re-plated and fixed up. As you can see below they were converted to H4 lamp socket. Actually, the foglights are slightly modified and have new reflectors from a tractor (unknown which) and H4 lamp feet coming from the /8 Mercedes for year 1973 and younger.
Before re-chroming I drilled out all riveted parts. The base of the fog light is not chromed. Since I don’t have good enough cleaning equipment, I decided to polish the base and then have it “white cadmium”, hoping that it’s luster will go down rather quickly. Grinding them would not be an option since that would be visible after the plating.
Step-by-step they will reach their restored, final look. Below the re-chromed pot and ornamental rings.
Having all parts in place, the assembly could start. First the light pot was rust protected with a thick Tectyl where the base was to sit. After hat the base was greased and then put in place together with the vertical screw and its holder. Everything was riveted with 5 mm DIN 660 aluminum rivets. Then the small bracket that holds the ornamental ring in place was riveted with 4 mm DIN 660 aluminum rivets.
Next step was to fixate lamp with sealing ring into the chromed ornamental ring with the help of 5 retaining springs. Before the assembly I altered the lamp feet. As you can see in the pictures above the lamp feet originally had their wires soldered. I preferred to have the electrical wires coming from the main cable harness to be easily pressed into, and also removed from, the contacts instead. So the old contacts were drilled out and replaced with suitable contacts which were riveted with DIN 660 aluminum rivets. Then it was just to mount the correct base plate, washers, rubber sealing etc and I was done. I’m very pleased with the result.
Rotary switch
This has a very short write up under the "Instruments and switches" (group 54) where I decided to collect all instrument panel stuff.